Summary for Test 2022-09-15-22-1

Test performed: CTM 216-June 2011

Project Information

Project IdentifiersProject ID: 212246
DEA: 053307A4
EFIS: 0514000027
DIST-CO-RTE-PM05-SLO-46-49.7/54.6
Award DateNot set
Closeout DateNot set
Work DescriptionCholame Segment
Location DescriptionNot set
QA Service Level1 (Verified on 09/30/2019)

Sample Information

Sample Taken Date09/15/2022 Sample Unique Key22
Will the laboratory/organization for which you are a member perform testing on this material sample?Yes Date that the sample was received by the laboratory/organization performing the testing09/15/2022
Sample typeQuality Assurance A brief description of the sampleClass 1 ASB from roadway
The quantity of what the sample constitutes1099+00 - 1102+46 @ 52' Wide From where was the sample collectedJob Site
First name of sampler or witnessed byKyle Last name of sampler or witnessed byEngen
Title of samplerTET Telephone number of sampler8055409933
Laboratory sample identification37057CL1ASB3 Linked DIME Sample ID
The fabricator/manufacturer/facility nameSPM Avenal Plant Transportation Laboratory (TL) Number
Inspector Lot Number from the Transportation Laboratory (TL) Form Structure unique identifier
Structure name

Material Information

Material TypeAggregate Source Identification (SMARA, name of Pit or Job Site)91-10-0006
The fabricator's/manufacturer's product name for the sample The fabricator/manufacturer designation for the sample
The plant number A detailed description of where the material sample was collectedJobsite-windrow
Where the material sample would have been placed if not sampled Primary Aggregate Nominal Size1-1/2 inch
The concrete mix design number Lot number
Sublot number Aggregate Mix NumberNot set

Test Details

DIME Sample ID: 2022-09-15-22
DIME Test ID: 2022-09-15-22-1
Testing Lab: CT D05 - Whitley Gardens Field Laboratory
Test Method: CTM 216-June 2011: Method of Test for Relative Compaction of Untreated and Treated Soils and Aggregates
Test Release Date: 2022-09-15

Test Results


Is oversize material: Yes
Input Type: Measured
Tester's full name: Kyle Engen
Date of test: 09/15/2022
In-place wet density: 2.35
Percentage passing 3/4 in. sieve: 89 %
Percentage retained on 3/4 in. sieve: 11 %
Specific gravity of material passing 3/4 in. sieve: 2.35
Specific gravity of material retained on 3/4 in. sieve: 2.6 %
% Moisture: no data
Optimum Moisture: no data
Coefficient for 3/4 in. aggregate: 1.00
Corrected density: 2.38
Relative compaction: 99
General comments (publicly viewable) (Max 1000 characters):

Test File Attachments

File NameExtensionFile SizeDate UploadedTest IDActions
05-3307A4_37057_220915_BLW_ASB_1099+00-1102+66_1pdf209.18 KB09/15/20222022-09-15-22-1   Info

Test was verified on 9/15/2022