Summary for Test 2020-03-19-11-2
Test performed: AASHTO T30-19Project Information
Project Identifiers | Project ID: 213469 DEA: 024C40V4 EFIS: 0218000125 |
---|---|
DIST-CO-RTE-PM | 02-SHA-5-R3.8/R11.7 |
Award Date | 11/06/2018 |
Closeout Date | 08/16/2023 |
Work Description | WIDEN TO 6 LANES, BRIDGE REPLACEMENT AND WIDENING AND ROADWAY REHAB |
Location Description | SHASTA COUNTY IN AND NEAR ANDERSON FROM ROUTE 5/273 SEPARATION TO 0.4 MILE SOUTH OF CHURN CREEK ROAD OVERCROSSING |
QA Service Level | 1 (Verified on 12/31/2018) |
Sample Information
Sample Taken Date | 03/19/2020 | Sample Unique Key | 11 |
---|---|---|---|
Will the laboratory/organization for which you are a member perform testing on this material sample? | Yes | Date that the sample was received by the laboratory/organization performing the testing | 03/20/2020 |
Sample type | Verification | A brief description of the sample | RAP |
The quantity of what the sample constitutes | JMF Renewal | From where was the sample collected | Manufacturer |
First name of sampler or witnessed by | Karen | Last name of sampler or witnessed by | Spliethof |
Title of sampler | TET | Telephone number of sampler | |
Laboratory sample identification | D78360B | Linked DIME Sample ID | 2020-03-19-10 |
The fabricator/manufacturer/facility name | Fawndale Rock and Asphalt - Redding, CA | Transportation Laboratory (TL) Number | 001698 |
Inspector Lot Number from the Transportation Laboratory (TL) Form | Structure unique identifier | ||
Structure name |
Material Information
Material Type | Reclaimed Asphalt Pavement | RAP Source | Fawndale Rock and Asphalt, Redding, CA |
---|---|---|---|
Aggregate Size | 3/8-inch | Aggregate Source | Unknown |
RAP Stockpile | Stockpile Size (tons) | Unknown | |
Reclaimed Asphalt Pavement Mix Number | Not set |
Test Details
DIME Sample ID: 2020-03-19-11
DIME Test ID: 2020-03-19-11-2
Testing Lab: CT D02 - Redding Northern Regional Laboratory
Test Method: AASHTO T30-19: Standard Method of Test for Mechanical Analysis of Extracted Aggregate (Mechanical Analysis)
Test Release Date: 2020-04-07
Test Results
Does this test use 1/4 sieve?: Yes
Is an aggregate correction factor used?: No
Input Type: Measured
Tester's full name: Karen Spliethof
Date of test: 03/24/2020
Cumulative Mass Retained | Cumulative Percent Passing | |||||
---|---|---|---|---|---|---|
1,317.8 grams | ||||||
0.0 grams | 100 % | |||||
0.0 grams | 100 % | |||||
0.0 grams | 100 % | |||||
0.0 grams | 100 % | |||||
0.0 grams | 100 % | |||||
18.0 grams | 98.6 % | |||||
231.7 grams | 82.4 % | |||||
421.1 grams | 68 % | |||||
717.6 grams | 45.5 % | |||||
893.5 grams | 32.2 % | |||||
1,004.2 grams | 23.8 % | |||||
1,081.7 grams | 17.9 % | |||||
1,113.6 grams | 15.5 % | |||||
1,176.4 grams | 10.7 % |
General comments (publicly viewable) (Max 1000 characters):
Test was verified on 4/7/2020 ✔