Summary for Test 2019-07-30-16-2
Test performed: AASHTO T30-19Project Information
Project Identifiers | Project ID: 213469 DEA: 024C40V4 EFIS: 0218000125 |
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DIST-CO-RTE-PM | 02-SHA-5-R3.8/R11.7 |
Award Date | 11/06/2018 |
Closeout Date | 08/16/2023 |
Work Description | WIDEN TO 6 LANES, BRIDGE REPLACEMENT AND WIDENING AND ROADWAY REHAB |
Location Description | SHASTA COUNTY IN AND NEAR ANDERSON FROM ROUTE 5/273 SEPARATION TO 0.4 MILE SOUTH OF CHURN CREEK ROAD OVERCROSSING |
QA Service Level | 1 (Verified on 12/31/2018) |
Sample Information
Sample Taken Date | 07/30/2019 | Sample Unique Key | 16 |
---|---|---|---|
Will the laboratory/organization for which you are a member perform testing on this material sample? | Yes | Date that the sample was received by the laboratory/organization performing the testing | 07/30/2019 |
Sample type | Verification | A brief description of the sample | Combined RAP, 3/8-inch |
The quantity of what the sample constitutes | JMF Verification | From where was the sample collected | Manufacturer |
First name of sampler or witnessed by | Colt | Last name of sampler or witnessed by | Sweeny |
Title of sampler | Telephone number of sampler | ||
Laboratory sample identification | D78055 | Linked DIME Sample ID | |
The fabricator/manufacturer/facility name | Fawndale Rock Quarry | Transportation Laboratory (TL) Number | 736161 |
Inspector Lot Number from the Transportation Laboratory (TL) Form | Structure unique identifier | ||
Structure name |
Material Information
Material Type | Reclaimed Asphalt Pavement | RAP Source | Fawndale Rock and Asphalt, Redding, CA |
---|---|---|---|
Aggregate Size | Combined, 3/8-inch | Aggregate Source | Unknown |
RAP Stockpile | Stockpile Size (tons) | Unknown | |
Reclaimed Asphalt Pavement Mix Number | Not set |
Test Details
DIME Sample ID: 2019-07-30-16
DIME Test ID: 2019-07-30-16-2
Testing Lab: CT D02 - Redding Northern Regional Laboratory
Test Method: AASHTO T30-19: Standard Method of Test for Mechanical Analysis of Extracted Aggregate (Mechanical Analysis)
Test Release Date: 2020-03-09
Test Results
Does this test use 1/4 sieve?: Yes
Is an aggregate correction factor used?: No
Input Type: Calculated
Tester's full name: Ward Jenkins
Date of test: 08/01/2019
Cumulative percent passing the 2 in. sieve: 100 %
Cumulative percent passing the 1 1/2 in. sieve: 100 %
Cumulative percent passing the 1 in. sieve: 100 %
Cumulative percent passing the 3/4 in. sieve: 100 %
Cumulative percent passing the 1/2 in. sieve: 100 %
Cumulative percent passing the 3/8 in. sieve: 97.4 %
Cumulative percent passing the 1/4 in. sieve: 79.1 %
Cumulative percent passing the #4 sieve: 67 %
Cumulative percent passing the #8 sieve: 47.1 %
Cumulative percent passing the #16 sieve: 34.5 %
Cumulative percent passing the #30 sieve: 26 %
Cumulative percent passing the #50 sieve: 19.6 %
Cumulative percent passing the #100 sieve: 14.2 %
Cumulative percent passing the #200 sieve: 10.4 %
General comments (publicly viewable) (Max 1000 characters):
Test was verified on 3/9/2020 ✔