Summary for Test 2020-04-08-11-2
Test performed: AASHTO T30-19Project Information
| Project Identifiers | Project ID: 213469 DEA: 024C40V4 EFIS: 0218000125 |
|---|---|
| DIST-CO-RTE-PM | 02-SHA-5-R3.8/R11.7 |
| Award Date | 11/06/2018 |
| Closeout Date | 08/16/2023 |
| Work Description | WIDEN TO 6 LANES, BRIDGE REPLACEMENT AND WIDENING AND ROADWAY REHAB |
| Location Description | SHASTA COUNTY IN AND NEAR ANDERSON FROM ROUTE 5/273 SEPARATION TO 0.4 MILE SOUTH OF CHURN CREEK ROAD OVERCROSSING |
| QA Service Level | 1 (Verified on 12/31/2018) |
Sample Information
| Sample Taken Date | 04/08/2020 | Sample Unique Key | 11 |
|---|---|---|---|
| Will the laboratory/organization for which you are a member perform testing on this material sample? | Yes | Date that the sample was received by the laboratory/organization performing the testing | 04/08/2020 |
| Sample type | Verification | A brief description of the sample | Combined RAP, -3/8-inch |
| The quantity of what the sample constitutes | JMF Renewal | From where was the sample collected | Manufacturer |
| First name of sampler or witnessed by | Karen | Last name of sampler or witnessed by | Spliethof |
| Title of sampler | Telephone number of sampler | ||
| Laboratory sample identification | D78376B | Linked DIME Sample ID | |
| The fabricator/manufacturer/facility name | Fawndale Rock and Asphalt | Transportation Laboratory (TL) Number | 897563 |
| Inspector Lot Number from the Transportation Laboratory (TL) Form | Structure unique identifier | ||
| Structure name | Bid Item | Not set |
Material Information
| Material Type | Reclaimed Asphalt Pavement | RAP Source | Fawndale Rock and Asphalt |
|---|---|---|---|
| Aggregate Size | 3/8-inch | Aggregate Source | Unknown |
| RAP Stockpile | Stockpile Size (tons) | Unknown | |
| Reclaimed Asphalt Pavement Mix Number | Not set |
Test Details
DIME Sample ID: 2020-04-08-11
DIME Test ID: 2020-04-08-11-2
Testing Lab: CT D02 - Redding Northern Regional Laboratory
Test Method: AASHTO T30-19: Standard Method of Test for Mechanical Analysis of Extracted Aggregate (Mechanical Analysis)
Test Release Date: 2020-05-19
Test Results
Does this test use 1/4 sieve?: Yes
Is an aggregate correction factor used?: No
Input Type: Measured
Tester's full name: Karen Spliethof
Date of test: 04/10/2020
| Cumulative Mass Retained | Cumulative Percent Passing | |||||
|---|---|---|---|---|---|---|
| 1478.0 grams | ||||||
| 0.0 grams | 100 % | |||||
| 0.0 grams | 100 % | |||||
| 0.0 grams | 100 % | |||||
| 0.0 grams | 100 % | |||||
| 0.0 grams | 100 % | |||||
| 13.7 grams | 99.1 % | |||||
| 222.7 grams | 84.9 % | |||||
| 494.1 grams | 66.6 % | |||||
| 709.5 grams | 52 % | |||||
| 928.5 grams | 37.2 % | |||||
| 1078.2 grams | 27.1 % | |||||
| 1186.3 grams | 19.7 % | |||||
| 1261.2 grams | 14.7 % | |||||
| 1310.6 grams | 11.3 % | |||||
General comments (publicly viewable) (Max 1000 characters):
Test was verified on 5/19/2020 ✔
