Summary for Test 2026-06-17-17-3

Test performed: AASHTO T30-25

Project Information

Project IdentifiersProject ID: 1001669
DEA: 09379004
EFIS: 0919000004
DIST-CO-RTE-PM09-INY-395-R65.0/76.0
Award Date12/24/2025
Closeout DateNot set
Work DescriptionFULL DEPTH RECYCLING, COLD PLANE, HMA AND CURB RAMPS.
Location DescriptionINYO COUNTY AT AND NEAR INDEPENDENCE FROM 3 MILES SOUTH OF MANZANAR REWARD ROAD TO 0.3 MILE NORTH OF SHABBELL LANE
QA Service Level1 (Verified on 10/13/2025)

Sample Information

Sample Taken Date06/17/2026 Sample Unique Key17
Will the laboratory/organization for which you are a member perform testing on this material sample?Yes Date that the sample was received by the laboratory/organization performing the testing06/17/2026
Sample typeAcceptance A brief description of the sample1500 - 2250 tons for today
The quantity of what the sample constitutes12 boxes of 3/4" Type A HMA with RAP From where was the sample collectedJob Site
First name of sampler or witnessed byJeff Last name of sampler or witnessed byPuente
Title of sampler Telephone number of sampler
Laboratory sample identificationHMA - 18 Linked DIME Sample ID
The fabricator/manufacturer/facility nameGrinding Rock - Independence Transportation Laboratory (TL) Number
Inspector Lot Number from the Transportation Laboratory (TL) Form Structure unique identifier
Structure name Bid Item3953633

Material Information

Material TypeHot Mix Asphalt HMA TypeType A HMA
HMA Grading3/4 inch Lot number1
Sublot number18 HMA Mix Number
Binder content (%)0.0 Virgin binder PG
Design binder PG Binder Supplier
RAP content (%)18 WMA Additives
Antistrip type

Test Details

DIME Sample ID: 2026-06-17-17
DIME Test ID: 2026-06-17-17-3
Testing Lab: CT D09 - Bishop Field Laboratory
Test Method: AASHTO T30-25: Standard Method of Test for Mechanical Analysis of Extracted Aggregate (Mechanical Analysis)
Test Release Date: 2026-06-22

Test Results


Individual or cumulative mass retained on each sieve?: Cumulative
Has the fine aggregate sample been reduced?: No
Is an aggregate correction factor used?: Yes
Was the aggregate obtained using ASTM D8159?: No
Input Type: Measured
Tester's full name: Derek Carrington
Date of test: 06/18/2026
Total mass of material in the sample: 2121.2 grams
Aggregate correction factor for the 2 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 1 1/2 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 1 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 3/4 in. sieve (% passing): -1.0 %
Aggregate correction factor for the 1/2 in. sieve (% passing): -0.2 %
Aggregate correction factor for the 3/8 in. sieve (% passing): -0.3 %
Aggregate correction factor for the #4 sieve (% passing): -1.1 %
Aggregate correction factor for the #8 sieve (% passing): -1.2 %
Aggregate correction factor for the #16 sieve (% passing): -0.9 %
Aggregate correction factor for the #30 sieve (% passing): -0.7 %
Aggregate correction factor for the #50 sieve (% passing): -0.5 %
Aggregate correction factor for the #100 sieve (% passing): -0.2 %
Aggregate correction factor for the #200 sieve (% passing): -0.1 %
General comments (publicly viewable) (Max 1000 characters): HMA-18 PP Gradation

Test was verified on 6/22/2026