Summary for Test 2026-06-11-6-2

Test performed: AASHTO T30-25

Project Information

Project IdentifiersProject ID: 1002310
DEA: 010P6404
EFIS: 0125000053
DIST-CO-RTE-PM01-HUM-101-R131.7/134.6
Award Date02/17/2026
Closeout DateNot set
Work DescriptionBoyes Creek Viaduct
Location DescriptionNot set
QA Service LevelNOT VERIFIED

Sample Information

Sample Taken Date06/11/2026 Sample Unique Key6
Will the laboratory/organization for which you are a member perform testing on this material sample?Yes Date that the sample was received by the laboratory/organization performing the testing06/11/2026
Sample typeQuality Assurance A brief description of the sample1/2 RHMA PG 64-16
The quantity of what the sample constitutes4 boxs From where was the sample collectedManufacturer
First name of sampler or witnessed byJacob Last name of sampler or witnessed byKnipscheer
Title of sampler Telephone number of sampler
Laboratory sample identification Linked DIME Sample ID
The fabricator/manufacturer/facility nameMercer Fraser Boyd Road Transportation Laboratory (TL) Number
Inspector Lot Number from the Transportation Laboratory (TL) Form Structure unique identifier
Structure name Bid ItemNot set

Material Information

Material TypeHot Mix Asphalt HMA TypeRHMA-G
HMA Grading1/2 inch Lot number
Sublot number HMA Mix Number
Binder content (%)0.0 Virgin binder PG
Design binder PG Binder Supplier
RAP content (%)Not set WMA Additives
Antistrip type

Test Details

DIME Sample ID: 2026-06-11-6
DIME Test ID: 2026-06-11-6-2
Testing Lab: CT D01 - Boyd Road Field Laboratory
Test Method: AASHTO T30-25: Standard Method of Test for Mechanical Analysis of Extracted Aggregate (Mechanical Analysis)
Test Release Date: 2026-06-12

Test Results


Individual or cumulative mass retained on each sieve?: Cumulative
Has the fine aggregate sample been reduced?: No
Is an aggregate correction factor used?: Yes
Was the aggregate obtained using ASTM D8159?: No
Input Type: Measured
Tester's full name: jacob Knipscheer-costello
Date of test: 06/12/2026
Total mass of material in the sample: 1431.3 grams
Aggregate correction factor for the 2 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 1 1/2 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 1 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 3/4 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 1/2 in. sieve (% passing): 0.1 %
Aggregate correction factor for the 3/8 in. sieve (% passing): 0.0 %
Aggregate correction factor for the #4 sieve (% passing): 0.9 %
Aggregate correction factor for the #8 sieve (% passing): 1.5 %
Aggregate correction factor for the #16 sieve (% passing): 1.1 %
Aggregate correction factor for the #30 sieve (% passing): 0.8 %
Aggregate correction factor for the #50 sieve (% passing): 0.7 %
Aggregate correction factor for the #100 sieve (% passing): 0.6 %
Aggregate correction factor for the #200 sieve (% passing): 0.6 %
General comments (publicly viewable) (Max 1000 characters): #8 & #200 are out of specification limits

Test was verified on 6/12/2026