Summary for Test 2026-04-22-9-1

Test performed: AASHTO T30-25

Project Information

Project IdentifiersProject ID: 1000997
DEA: 010J2104
EFIS: 0118000190
DIST-CO-RTE-PM01-DN-101-R2.6/23.9
Award Date06/06/2025
Closeout DateNot set
Work DescriptionRHMA, HMA, AND COLD PLANE ASPHALT CONCRETE PAVEMENT.
Location DescriptionDEL NORTE COUNTY IN AND NEAR KLAMATH FROM 1.2 MILES SOUTH OF KLAMATH RIVER OVERFLOW TO 1.1 MILE NORTH OF HAMILTON ROAD
QA Service Level1 (Verified on 03/21/2025)

Sample Information

Sample Taken Date04/22/2026 Sample Unique Key9
Will the laboratory/organization for which you are a member perform testing on this material sample?Yes Date that the sample was received by the laboratory/organization performing the testing04/22/2026
Sample typeAcceptance A brief description of the sample1/2 HMA-A
The quantity of what the sample constitutes24 boxes From where was the sample collectedManufacturer
First name of sampler or witnessed byjason Last name of sampler or witnessed byhuett
Title of sampler Telephone number of sampler
Laboratory sample identification Linked DIME Sample ID
The fabricator/manufacturer/facility nameMercer Fraser Boyd Road Transportation Laboratory (TL) Number
Inspector Lot Number from the Transportation Laboratory (TL) Form Structure unique identifier
Structure name Bid ItemNot set

Material Information

Material TypeHot Mix Asphalt HMA TypeType A HMA
HMA Grading1/2 inch Lot number
Sublot number HMA Mix Number
Binder content (%)0.0 Virgin binder PG
Design binder PG Binder Supplier
RAP content (%)Not set WMA Additives
Antistrip type

Test Details

DIME Sample ID: 2026-04-22-9
DIME Test ID: 2026-04-22-9-1
Testing Lab: CT D01 - Crescent City Field Laboratory
Test Method: AASHTO T30-25: Standard Method of Test for Mechanical Analysis of Extracted Aggregate (Mechanical Analysis)
Test Release Date: 2026-04-23

Test Results


Individual or cumulative mass retained on each sieve?: Cumulative
Has the fine aggregate sample been reduced?: No
Is an aggregate correction factor used?: Yes
Was the aggregate obtained using ASTM D8159?: No
Input Type: Measured
Tester's full name: jason huett
Date of test: 04/23/2026
Total mass of material in the sample: 1541.8 grams
Aggregate correction factor for the 2 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 1 1/2 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 1 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 3/4 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 1/2 in. sieve (% passing): 0.1 %
Aggregate correction factor for the 3/8 in. sieve (% passing): -0.1 %
Aggregate correction factor for the #4 sieve (% passing): 0.5 %
Aggregate correction factor for the #8 sieve (% passing): 0.9 %
Aggregate correction factor for the #16 sieve (% passing): 1.4 %
Aggregate correction factor for the #30 sieve (% passing): 1.6 %
Aggregate correction factor for the #50 sieve (% passing): 1.1 %
Aggregate correction factor for the #100 sieve (% passing): 0.7 %
Aggregate correction factor for the #200 sieve (% passing): 0.2 %
General comments (publicly viewable) (Max 1000 characters):

Test File Attachments

File NameExtensionFile SizeDate UploadedTest IDActions
BoydContSuiteH@dot.ca.gov_20260423_073120pdf406.58 KB04/23/20262026-04-22-9-1   Info

Test was verified on 4/23/2026