Summary for Test 2026-04-20-15-5

Test performed: AASHTO T30-25

Project Information

Project IdentifiersProject ID: 1000541
DEA: 09374704
EFIS: 0918000019
DIST-CO-RTE-PM09-INY-168,395-17.6/18.3,114.9/117.8
Award Date02/21/2025
Closeout DateNot set
Work DescriptionHMA (TYPE A), MINOR CONCRETE, AND LIGHTING.
Location DescriptionINYO COUNTY IN AND NEAR BISHOP ON ROUTE 395 FROM 0.1 MILE SOUTH OF JAY STREET TO BARLOW LANE AND ON ROUTE 168 FROM PIONEER LANE TO ROUTE 395
QA Service Level1 (Verified on 09/02/2024)

Sample Information

Sample Taken Date04/20/2026 Sample Unique Key15
Will the laboratory/organization for which you are a member perform testing on this material sample?Yes Date that the sample was received by the laboratory/organization performing the testing04/20/2026
Sample typeProduction Start-Up A brief description of the sample3/4" HMA-A-SP PG70-10 R15
The quantity of what the sample constitutes750 Tons From where was the sample collectedSource
First name of sampler or witnessed byDylan Last name of sampler or witnessed byCarapazza
Title of samplerConsultant Telephone number of sampler
Laboratory sample identificationPSU 03 Linked DIME Sample ID
The fabricator/manufacturer/facility nameGranite 5 Bridges Plant Bishop Transportation Laboratory (TL) Number5287
Inspector Lot Number from the Transportation Laboratory (TL) Form Structure unique identifier
Structure name Bid ItemNot set

Material Information

Material TypeHot Mix Asphalt HMA TypeType A HMA
HMA Grading3/4 inch Lot number
Sublot number HMA Mix Number
Binder content (%)4.9 Virgin binder PG
Design binder PG Binder Supplier
RAP content (%)15 WMA Additives
Antistrip type

Test Details

DIME Sample ID: 2026-04-20-15
DIME Test ID: 2026-04-20-15-5
Testing Lab: CT D09 - Bishop Field Laboratory
Test Method: AASHTO T30-25: Standard Method of Test for Mechanical Analysis of Extracted Aggregate (Mechanical Analysis)
Test Release Date: 2026-04-21

Test Results


Individual or cumulative mass retained on each sieve?: Cumulative
Has the fine aggregate sample been reduced?: No
Is an aggregate correction factor used?: Yes
Was the aggregate obtained using ASTM D8159?: Yes
Input Type: Measured
Tester's full name: Derek Carrington
Date of test: 04/21/2026
Total mass of material in the sample: 2095.4 grams
Aggregate correction factor for the 2 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 1 1/2 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 1 in. sieve (% passing): 0.0 %
Aggregate correction factor for the 3/4 in. sieve (% passing): 1.0 %
Aggregate correction factor for the 1/2 in. sieve (% passing): -2.5 %
Aggregate correction factor for the 3/8 in. sieve (% passing): -2.7 %
Aggregate correction factor for the #4 sieve (% passing): -4.8 %
Aggregate correction factor for the #8 sieve (% passing): -3.5 %
Aggregate correction factor for the #16 sieve (% passing): -2.7 %
Aggregate correction factor for the #30 sieve (% passing): -2.6 %
Aggregate correction factor for the #50 sieve (% passing): -2.0 %
Aggregate correction factor for the #100 sieve (% passing): -1.1 %
Aggregate correction factor for the #200 sieve (% passing): -1.9 %
Mineral Matter in Centrifuge Cup (D8159 only): 0.0 grams
Initial Specimen Mass: 2095.4 grams
General comments (publicly viewable) (Max 1000 characters): PSU 03

Test was verified on 4/21/2026