Summary for Test 2025-10-19-8-1

Test performed: CTM 524-March 2013

Project Information

Project IdentifiersProject ID: 993825
DEA: 040Q30U4
EFIS: 0420000235
COOP: 042830A3,042830A4
DIST-CO-RTE-PM04-ALA,CC-680-R11.0/R21.9,R0.0/R0.9
Award Date11/23/2022
Closeout DateNot set
Work DescriptionPRECAST CONC PVMT, ELECTRONIC TOLL SYSTEM, JPCP, CB & STRUCTURAL CONC
Location DescriptionALAMEDA AND CONTRA COSTA COUNTIES AT SUNOL AND IN SAN RAMON BETWEEN 0.4 MILE SOUTH OF CALAVERAS ROAD UNDERCROSSING TO 0.9 MILE NORTH OF ALCOSTA BOULEVARD OVERCROSSING
QA Service Level1 (Verified on 05/11/2022)

Sample Information

Sample Taken Date10/19/2025 Sample Unique Key8
Will the laboratory/organization for which you are a member perform testing on this material sample?Yes Date that the sample was received by the laboratory/organization performing the testing10/19/2025
Sample typeQuality Assurance A brief description of the sample3 Day Beam Breaks
The quantity of what the sample constitutes3 Beams From where was the sample collectedJob Site
First name of sampler or witnessed byChristian Last name of sampler or witnessed bySouza
Title of sampler Telephone number of sampler
Laboratory sample identification Linked DIME Sample ID
The fabricator/manufacturer/facility nameCemex Antioch Transportation Laboratory (TL) Number
Inspector Lot Number from the Transportation Laboratory (TL) Form Structure unique identifier
Structure name Bid ItemNot set

Material Information

Material TypeRapid Set ManufacturerCemex Antioch
Mix no.1630479 Materials Received3 Beams
Lot no.1 Batch Number1

Test Details

DIME Sample ID: 2025-10-19-8
DIME Test ID: 2025-10-19-8-1
Testing Lab: CT D04 - Richmond Field Laboratory
Test Method: CTM 524-March 2013: Method of Test for Flexural Strength Of Rapid Strength Concrete
Test Release Date: 2025-10-23

Test Results


Number of specimens: 3
Does the testing machine measure load or stress on the beam specimen?: Load
Fracture initiates in the tension surface: Within the Middle Third of the Span Length
Fracture occurred at a capped section: No
Is a beam dimensional correction factor used?: No
Input Type: Measured
Tester's full name: Jose Leon Amparan
Date of test: 10/22/2025
Identification number: 3 Day Break
Width of specimen: 6 inch
Width of specimen 2: 6 inch
Width of specimen 3: 6.125 inch
Depth of specimen: 6 inch
Depth of specimen 2: 6.1875 inch
Depth of specimen 3: 6.1875 inch
Span length of specimen: 21 inch
Span length of specimen 2: 21 inch
Span length of specimen 3: 21 inch
Maximum load applied: 7010 lb
Maximum load applied 2: 8100 lb
Maximum load applied 3: 9900 lb
Curing history and apparent moisture condition of the specimen: 3 Days , In water bath
If specimen was capped, ground or if leather shims were used: Leather Shims were used
Defects in specimen, including numbers of beams discarded during test: N/A
Age of specimen: 3 days
Age of specimen in hours: 77 hours
Modulus of rupture: 720 psi
Modulus of rupture 2: 780 psi
Modulus of rupture 3: 930 psi
Modulus of rupture average: 810 psi
General comments (publicly viewable) (Max 1000 characters): 3 Day Break

Test was verified on 10/23/2025