Summary for Test 2025-09-02-65-2

Test performed: AASHTO T30-19

Project Information

Project IdentifiersProject ID: 1000901
DEA: 061G8004
EFIS: 0624000167
DIST-CO-RTE-PM06-KER-99-R29.4/33.1
Award Date03/27/2025
Closeout DateNot set
Work DescriptionCOLD PLANE AC PAVEMENT, REMOVE CONCRETE PAVEMENT, AND HMA.
Location DescriptionKERN COUNTY NEAR BAKERSFIELD FROM 0.5 MILE SOUTH OF ROUTE 65/99 SEPARATION TO 0.7 MILE NORTH OF LERDO CANAL BRIDGE
QA Service Level1 (Verified on 01/22/2025)

Sample Information

Sample Taken Date09/02/2025 Sample Unique Key65
Will the laboratory/organization for which you are a member perform testing on this material sample?Yes Date that the sample was received by the laboratory/organization performing the testing09/03/2025
Sample typeAcceptance A brief description of the sample1/2" RHMA- Type O
The quantity of what the sample constitutesL2SL6 From where was the sample collectedSource
First name of sampler or witnessed byQC Last name of sampler or witnessed byG3
Title of samplerMaterials Tester Telephone number of sampler
Laboratory sample identification Linked DIME Sample ID
The fabricator/manufacturer/facility nameGriffith Edmonston Transportation Laboratory (TL) Number
Inspector Lot Number from the Transportation Laboratory (TL) Form Structure unique identifier
Structure name Bid ItemNot set

Material Information

Material TypeAggregate Source Identification (SMARA, name of Pit or Job Site)91-15-0068::GRIFFITH COMPANY
The fabricator's/manufacturer's product name for the sample The fabricator/manufacturer designation for the sample
The plant number A detailed description of where the material sample was collectedHMA Plant Cold Feed
Where the material sample would have been placed if not sampled Primary Aggregate Nominal Size1/2 inch
The concrete mix design number Lot number2
Sublot number6 Aggregate Mix Number

Test Details

DIME Sample ID: 2025-09-02-65
DIME Test ID: 2025-09-02-65-2
Testing Lab: CT D06 - Bakersfield Field Laboratory
Test Method: AASHTO T30-19: Standard Method of Test for Mechanical Analysis of Extracted Aggregate (Mechanical Analysis)
Test Release Date: 2025-09-03

Test Results


Does this test use 1/4 sieve?: No
Is an aggregate correction factor used?: Yes
Input Type: Measured
Tester's full name: Alex
Date of test: 09/03/2025
Cumulative Mass RetainedCorrection FactorCumulative Percent Passing
1454.8 grams
0.0 grams0.0 %100 %
0.0 grams0.0 %100 %
0.0 grams0.0 %100 %
0.0 grams0.0 %100 %
40.1 grams0.0 %97 %
252.1 grams-0.5 %82 %
898.8 grams0.6 %39 %
1220.8 grams-0.3 %16 %
1334.1 grams-0.4 %8 %
1334.1 grams-0.5 %8 %
1363.5 grams-0.4 %6 %
1388.0 grams0.3 %5 %
1406.4 grams0.1 %3.4 %
1410.1 grams
General comments (publicly viewable) (Max 1000 characters):

Test File Attachments

File NameExtensionFile SizeDate UploadedTest IDActions
06-1G8004_37015_250903_L2SL6_T30.pdf117.88 KB09/03/20252025-09-02-65-2   Info

Test was verified on 9/3/2025