Summary for Test 2022-07-11-64-3

Test performed: AASHTO T30-19

Project Information

Project IdentifiersProject ID: 993623
DEA: 022J3704
EFIS: 0221000071
DIST-CO-RTE-PM02-SHA-299-50.5/56.5,93.5/99.3
Award Date04/29/2022
Closeout Date10/06/2022
Work DescriptionASPHALT RUBBER BINDER SEAL COAT, COLD PLANE AC PAVEMENT AND HMA.
Location DescriptionSHASTA COUNTY NEAR MONTGOMERY CREEK FROM 0.2 MILE WEST OF OAK POINT DRIVE TO OLD BERTAGNA PLACE AND FROM 0.1 MILE EAST OF SIERRA CENTER DRIVE TO LASSEN COUNTY LINE
QA Service Level1 (Verified on 03/18/2022)

Sample Information

Sample Taken Date07/11/2022 Sample Unique Key64
Will the laboratory/organization for which you are a member perform testing on this material sample?Yes Date that the sample was received by the laboratory/organization performing the testing07/11/2022
Sample typeDepartment Acceptance A brief description of the sampleCombined RAP
The quantity of what the sample constitutesProduction Start-Up Evaluation From where was the sample collectedManufacturer
First name of sampler or witnessed byCindy Last name of sampler or witnessed byBryant
Title of samplerTET Telephone number of sampler
Laboratory sample identificationD79086B Linked DIME Sample ID2022-07-11-62, 2022-07-11-63
The fabricator/manufacturer/facility nameJ.F. Shea Construction - Fawndale Rock and Asphalt - Redding, CA Transportation Laboratory (TL) Number867311
Inspector Lot Number from the Transportation Laboratory (TL) Form Structure unique identifier
Structure name

Material Information

Material TypeReclaimed Asphalt Pavement RAP SourceFawndale Rock and Asphalt, Redding, CA
Aggregate Size3/8 inch Aggregate Source
RAP Stockpile Stockpile Size (tons)
Reclaimed Asphalt Pavement Mix NumberNot set

Test Details

DIME Sample ID: 2022-07-11-64
DIME Test ID: 2022-07-11-64-3
Testing Lab: CT D02 - Redding Northern Regional Laboratory
Test Method: AASHTO T30-19: Standard Method of Test for Mechanical Analysis of Extracted Aggregate (Mechanical Analysis)
Test Release Date: 2022-07-28

Test Results


Does this test use 1/4 sieve?: Yes
Is an aggregate correction factor used?: No
Input Type: Measured
Tester's full name: Khue Yang
Date of test: 07/15/2022
Cumulative Mass RetainedCumulative Percent Passing
1507.9 grams
0 grams100 %
0 grams100 %
0 grams100 %
0 grams100 %
0 grams100 %
27 grams98.2 %
329.3 grams78.2 %
528.9 grams64.9 %
851 grams43.6 %
1044.1 grams30.8 %
1170.5 grams22.4 %
1263.7 grams16.2 %
1327.8 grams11.9 %
1367.5 grams9.3 %
General comments (publicly viewable) (Max 1000 characters):

Test was verified on 7/28/2022